Intelligent Engineering
Automation Platform

Version
2.0 Enhanced
Date
April 2026
Screens
15 screens
Status
Proposal
Dashboard
Design Guide
DFM Engine
Revision Intelligence
AI Co-Pilot
3D Unity Viewer
Knowledge Base
Design Review Sessions ★
Auto Knowledge Graph ★
Cost Estimation ★
External Portal ★
Mobile App ★
Customer Portal ★
Cross-Site R&D ★
Roadmap

Engineering operations dashboard

Real-time overview for engineering managers and leads

IEA Platform
Hoki Digital · v2.0
Main
◉ Dashboard
◈ Projects
◧ Items
Core modules
Design guide
DFM engine
Revision intelligence
3D viewer
Knowledge base
New v2.0
Review sessions NEW
Knowledge graph NEW
Cost engine NEW
Mobile app NEW
Operations
Tasks
Audit log
Active projects
14
3 with open DFM issues
DFM validations
87
This month
Effort saved
62%
vs manual baseline
Open tasks
23
8 high priority
Review sessions NEW
5
2 pending sign-off
Knowledge graph NEW
1,247
Nodes auto-captured
Recent activity
DFMP-4421 Rev C validated — 3 issues1h ago
ReviewDesign review session signed off2h ago
RevisionRev C vs B comparison complete3h ago
KGraph47 new knowledge nodes captured4h ago
NCRNCR-2024-0094 linked to DFM finding5h ago
Module usage this week
ModuleRunsAvg saved
DFM engine2447 min
Revision intelligence1832 min
AI co-pilot6112 min
Review sessions NEW965 min
Cost engine NEW1428 min
Open high-priority issues
PartIssueModuleAssignedStatus
P-5501Thin wall <0.8mm — linked to NCR-0091DFMS. PatelOpen
P-4421Bore tol. tightened — process riskRevisionJ. WongIn review
P-6001Undercut — cost impact: +18%Cost EngineR. KumarOpen

Intelligent design guide

Guided 5-step feasibility workflow — pre-sales through engineering

Design guide
Guided feasibility
Steps
1 Requirements
2 Geometry
3 Material
4 Process constraints
5 Feasibility + cost
Project
P-6001 · Customer A
Prototype run · Phase 1
1
2
3
4
5
Step 4 — process constraints
Machining process
Machine available
Surface finish required
Batch quantity
Tightest tolerance
Inspection standard
AI constraint check: M-05 Cpk 1.18 for this bore tolerance — below 1.33 required. Recommend M-07. Ra 0.8 needs polishing pass.
Cost preview NEW: Estimated machining cost for 50 pcs: S$4,200–5,100 (M-07, 316L, ±0.03mm bore). Removing undercut reduces this by ~12%. View cost breakdown
Inputs so far
P-6001 · Customer A
Bore Ø100, OD Ø140, 316L
Similar past jobs
P-4421 Rev C
316L · M-07 · 2024 · S$4,150
Successful
P-4422 Rev B
316L · M-07 · 2023 · S$3,920
NCR raised

Intelligent DFM engine

Automated manufacturability — with machine-specific Cpk routing and NCR linkage

DFM engine
Automated manufacturability
Queue
P-6001 Rev A 3 issues
P-4421 Rev C
P-5501 Rev B 1 issue
Rules library
Wall thickness rules
Undercut detection
Tolerance / Cpk rules ENHANCED
NCR linkage NEW
DFM report — P-6001 Rev A
3 issues found · 11 passed · 316L · 14 rules checked
3 issues11 passed
Enhanced in v2.0 ENHANCED: DFM results now include a colour heatmap on the 3D model surface (green/amber/red continuous gradient), machine-specific Cpk routing, and automatic NCR linkage when issues reach production.
High — undercut geometry at inner profile
Cannot machine
12° undercut at Z-45mm unreachable with standard turning tools on M-07 or M-05. Recommend relief groove (see Case-2023-041). Cost impact if redesigned: −12% (S$504 saving per batch).
Rule: UC-001Zone: inner bore Z-45Cost delta: −S$504
High — wall thickness below 0.8mm
Rework risk
Rib at face B: 0.62mm — below minimum 0.8mm for 316L. Chatter and deflection risk.
Rule: WT-003Zone: face B ribAuto-linked to NCR when in production
Medium — bore ±0.03mm tolerance
Machine routing required
Bore tolerance ±0.03mm requires Cpk ≥ 1.33. M-05 Cpk = 1.18 (not suitable). M-07 Cpk = 1.48 (approved).
Rule: TOL-007M-05: Cpk 1.18 ✗M-07: Cpk 1.48 ✓Cpk routing
Passed checks (11)
Min feature sizePass
Material machinability indexPass
OD tolerance vs Cpk (M-07)Pass
Thread standard conformancePass
AI recommendations
Redesign undercut
Add 0.5mm relief groove. Saves S$504/batch. See Case-2023-041.
Route bore to M-07 only NEW
Cpk 1.48 on M-07 vs 1.18 on M-05. Update routing sheet.
Thicken rib to 1.0mm
Minimal geometry change. Re-run DFM after.
Proactive lessons NEW
Auto-surfaced: 3 relevant past cases found without searching
Case-2023-041 — undercut fix
P-4422 · Relief groove · Resolved Rev B
NCR-2023-0041 — thin wall
P-5501 · Wall 0.62mm · CAPA closed

Drawing revision intelligence

Automated change detection with impact flags

Revision intelligence
Change detection
Comparisons
P-4421 Rev B → Rev C
P-5501 Rev A → Rev B
P-6001 Rev A → Rev B
P-4421 — Rev B → Rev C change report
Rev BRev C
AI summary: Rev C tightens bore diameter by 40%, updates face A surface finish to Ra 0.8, and adds a post-cooldown inspection note. No geometry or material changes. Process and QC updates required before production.
Change table
FieldRev BRev CImpact
Bore diameter tolerance±0.05mm±0.03mmTightened
Face A surface finishRa 1.6Ra 0.8Tightened
Inspection noteNonePost-cooldown checkAdded
Material316L ASTM A276316L ASTM A276Unchanged
Process impact flags
Machining
Bore tol. tightened 40%. Route to M-07. Verify Cpk.
QC checklist
Add 2hr cooldown hold per SOP-QC-114.
Finishing
Ra 0.8 may need extra polishing pass on face A.

AI engineering co-pilot

Grounded in Sateco's approved internal documents — always cites sources

AI co-pilot
Decision support
Conversations
P-6001 DFM issues
316L tolerance history
FAI report Batch 7
Quick actions
Summarise report
Explain DFM result
Draft NCR response
Proactive lessons NEW
P-6001 — DFM discussionP-60013 open
Proactive lessons surfaced NEW: 3 relevant past cases auto-found — Case-2023-041 (undercut fix), NCR-2023-0041 (thin wall), SOP-MACH-007 (5-axis). No search needed.
JW
Explain the undercut issue on P-6001 and what similar cases we've had.
AI
The undercut at Z-45mm on P-6001 Rev A is a 12° inner profile unreachable with standard turning tools on M-07 or M-05. DFM-UC-001

We had the same issue on P-4422 Rev A in 2023. Resolution: 0.5mm relief groove — no functional impact. Customer A approved in 2 working days. Cost saving: S$504/batch. Case-2023-041
Case-2023-041
P-4422 · undercut resolved
DFM rule UC-001
Undercut detection spec
JW
Draft a customer-ready explanation for why this geometry is hard to machine.
AI
Draft — review before sending

"The current inner profile at Z-45mm includes an undercut angle preventing access with standard CNC turning tools. We recommend a minor geometry revision — adding a small relief groove — which would fully resolve this constraint with no impact on part function, and reduce unit cost by approximately 12%."
Sources cited
DFM report — P-6001
Rule UC-001 · today
DFM
Case-2023-041
P-4422 undercut fix
Knowledge

3D Unity viewer ENHANCED

WebGL-powered viewer with continuous DFM heatmap overlay on model surface

3D viewer — P-6001 Rev A 3 DFM issues
! Undercut ! Thin wall ! Deep hole High Med OK Heatmap Z X Y Unity WebGL · Continuous DFM heatmap overlay
DFM heatmap ENHANCED
High severity
Medium
Good geometry
View: P-6001-Rev-A.step · 2.4 MB
Part tree
▾ P-6001 Rev A
Inner bore
Face B rib
Top holes ×3
OD profile
Selected: inner bore
DiameterØ100mm
Tolerance±0.03mm
Heatmap● High
DFM: High severity
12° undercut — cannot machine standard.

Knowledge base

Centralised engineering repository with semantic search

Knowledge base
Categories
All knowledge
SOPs & work instructions
Past cases & NCRs
DFM rules library
Material specs
5 results · semantic search across 1,847 documents
Case-2023-041 — P-4422 undercut resolution
12° undercut resolved by adding 0.5mm relief groove. No functional impact. Customer A approved in 2 working days.
CaseP-4422316L
97%
DFM rule UC-001 — undercut detection
Detects inner profile undercuts exceeding 5° unreachable with standard turning tooling. Flags high severity.
DFM ruleGeometry
92%
SOP-MACH-007 — 5-axis setup for complex geometry
Work instruction for M-09 (5-axis) for parts with undercuts or compound angles.
SOP5-axisM-09
85%

Design review sessions NEW

Structured virtual review with sign-off, auto-minutes, and knowledge capture — closes the CL gap

New in v2.0: Formal design review sessions with structured issue tracking, real-time + async markup, digital sign-off workflow, and auto-generated meeting minutes. Every decision is automatically captured into the knowledge graph.
Review sessions
Structured approvals
Active sessions
P-4421 Rev C — QA review 3 open
P-6001 DFM review Signed off
FAI — Batch 7
Actions
+ New session
Review templates
P-4421 Rev C — QA design review
Session #DR-2024-041 · Initiated by J. Wong · 11 Apr 2024
In progress
1
Agenda set
Done
2
Files shared
Done
3
Review & markup
Active
4
Resolve issues
Pending
5
Sign-off
Pending
Session issues — open comments
BH
B. Hassan — Johor ManufacturingOpenProcess concern
Bore tolerance ±0.03mm — M-05 Cpk is 1.18, below required 1.33. Need to discuss or route to M-07 only.
AI
AI co-pilot — auto-drafted replyAUTO-DRAFT
Per Cpk data, M-07 holds 1.48 for this tolerance. Recommend routing all P-4421 bore ops to M-07. Updating routing sheet.
SP
S. Patel — QA EngineerPending
Ra 0.8 on face A — confirm polishing pass is in setup sheet before sign-off.
DN
D. Ng — Customer A (External)Awaiting
Confirm measurement method and calibration reference for bore and OD.
Reviewers & sign-off status
ReviewerOrganisationRoleStatus
JW
J. Wong
HQOriginatorApproved
SP
S. Patel
HQ — QAQA reviewerIn review
BH
B. Hassan
Johor MfgProcess eng.Query raised
DN
D. Ng
Customer AExternal QCNot started
Session details
Agenda
1. Bore tolerance sign-off
2. Surface finish confirmation
3. Customer measurement query
Files attached
Drawing P-4421 Rev C.pdf
DFM report Rev C.pdf
Auto-minutes preview NEW
Auto-generated on session close: attendees, all comments, decisions, action items, and sign-off status — exported as PDF.
Knowledge capture NEW
All decisions in this session will be auto-added to the knowledge graph on close. 4 new nodes estimated.

Auto knowledge graph NEW

Passively captures every DFM run, review session, and co-pilot decision — no manual effort

New in v2.0: Every engineering activity in IEA automatically populates this knowledge graph. No engineer needs to manually log a lesson — the system captures it from DFM results, revision comparisons, review sessions, and co-pilot Q&A.
Knowledge graph
Auto-built from all activity
Sources
All sources
From DFM runs
From review sessions
From revision comparisons
From co-pilot sessions
Filters
By part family
By process
By engineer
⚠ Decay alerts (3)
Total nodes
1,247
Auto-captured
From DFM runs
412
Issues + resolutions
From reviews
389
Decisions + sign-offs
From co-pilot
446
Q&A pairs
Decay alerts
3
Nodes >2 years old
Recent auto-captures
SourceNode capturedTime
DFMUndercut → relief groove fix · P-60011h ago
ReviewM-07 routing decision for ±0.03mm bore2h ago
RevisionRa 0.8 polishing pass requirement — P-44213h ago
Co-pilotCustomer explanation template — DFM undercut4h ago
Proactive surfacing — lessons at review time NEW
When a DFM run or review session opens, the 3 most relevant knowledge nodes are shown automatically — without the engineer searching.
Triggered bySurfaced lessonRelevance
DFM: undercut detectedRelief groove fix — P-442296%
DFM: thin wallCAPA wall thickness — P-550191%
Review: bore toleranceM-07 Cpk 1.48 routing decision89%
Knowledge decay alerts 3 items need review
NodeAgeLast validatedAction
SOP-QC-114 tolerance hold time2.3 yearsJan 2022
M-05 Cpk baseline for bore ±0.05mm2.1 yearsMar 2022
316L machinability index — Tool life2.0 yearsApr 2022

Cost estimation engine NEW

Rough machining cost from Sateco's own ERP data — shown alongside DFM results

New in v2.0: Closes the gap vs PL ProDesk which shows instant cost estimates with DFM. IEA's cost engine uses Sateco's own ERP data — not generic market rates — making it accurate for Sateco's specific machines, materials, and processes.
Cost engine
ERP-linked estimation
Recent estimates
P-6001 Rev A · 50 pcs
P-4421 Rev C · 100 pcs
P-5501 Rev B · 25 pcs
Settings
Machine rates (ERP)
Material costs (ERP)
Setup time library
P-6001 Rev A — cost estimate
50 pcs · 316L · M-07 (Mazak) · ±0.03mm bore · Ra 0.8 face A
Total estimate
S$4,620
For 50 pcs (±15%)
Unit cost
S$92.40
Per piece
Machine hours
18.5 hr
M-07 @ S$180/hr
Similar past job
S$4,150
P-4421 · 50 pcs · 2024
Cost breakdown
ComponentHours/QtyRateCost (S$)
Material (316L bar)8.5 kgS$85/kg722
Turning (M-07)12.0 hrS$180/hr2,160
Milling (M-07)4.5 hrS$180/hr810
Polishing (Ra 0.8)2.0 hrS$90/hr180
Setup & fixturing1× batchS$320 flat320
Inspection (CMM)2.5 hrS$100/hr250
Total (50 pcs)4,442
Scenario comparison — DFM fixes
ScenarioΔ CostΔ Time
Current (with undercut) S$4,442 Baseline
Fix undercut (relief groove) S$3,938 (−11%) −2.5 hr
Use 5-axis (M-09) instead S$5,120 (+15%) +3.0 hr
Relax bore to ±0.05mm S$4,120 (−7%) −1.5 hr
Recommendation: Fixing the undercut saves S$504/batch (11%) and removes the highest-severity DFM issue. Optimal scenario.

Customer portal NEW

Secure external collaboration with customers — shared threads, drawing approvals, document firewall

External portal
Precision Co. → Customer A
Active projects
Batch 7 — P-4421
Batch 6 — P-5501
Prototype — P-6001
Documents shared
Drawing approvals
FAI reports
CoC / material certs
Delivery schedule
Batch 7 — P-4421 shared threadCustomer AActive
CA
Customer A — D. Ng · 09:14
Can you confirm Rev C approval and share the updated FAI report for Batch 7? Need it for our incoming QC by Friday.
JW
J. Wong · 09:31
Hi David — Rev C approved 28 Mar. FAI report and CoC attached below.
FAI-B7-P4421.pdfCoC-316L-Batch7.pdf
CA
Customer A — D. Ng · 10:02
Bore tolerance changed ±0.05 → ±0.03 in Rev C. Can you confirm your Cpk supports this?
AI
AI draft (review before sending) AUTO-DRAFT
M-07 Cpk = 1.48 for ±0.03mm bore (last 60 parts, Jan–Mar 2024), above 1.33 threshold. SPC chart available on request.
Shared with customer
Drawing P-4421 Rev C
Approved · 28 Mar
Shared
FAI report — Batch 7
Shared today
Shared
Blocked — document firewall NEW
Internal NCR-2024-0087
Auto-blocked — internal only
Restricted
SPC data — M-07
Pending approval to share
Pending

Cross-site R&D workspace NEW

Multi-site collaboration across HQ Singapore, Munich R&D, Johor Manufacturing, Osaka (observer)

R&D workspace
Cross-site collaboration
Sites
HQ — Singapore
R&D — Munich
Manufacturing — Johor
Lab — Osaka (observer)
Projects
Next-gen alloy — P-6001
Surface coating study
Next-gen alloy study — P-6001
R&D3 sites active
Experiments
48
Across 3 sites
Open questions
7
2 awaiting Munich
Cross-site docs
14
Shared
Site contributions
SiteExperimentsLatest
HQ — SG
18Today
Munich
22Yesterday
Johor
82d ago
Osaka
ObserverRead-only
Open questions
QuestionFromStatus
Optimal annealing temp — variant 3?HQAwaiting Munich
Ra 0.4 feasible after coating?MunichIn progress
Machinability vs 316L?JohorAnswered
AI synthesis — cross-site summary NEW
AI synthesis · updated 2h ago · based on 31 shared documents across 3 sites
Munich's annealing trials (Exp 19–22) show variant 3 achieves optimal hardness at 1,080°C for 45 min, outperforming variant 1 by 12% on tensile strength. HQ machining data confirms higher tool wear rate — Johor should validate with CNC setup before committing to production parameters.
Munich Exp-22.pdfHQ machining log AprAlloy variant 3 spec
Recent cross-site messages
MN
Munich — M. Neuer · 08:40
Exp-22 results uploaded. Variant 3 — Vickers 310 HV.
JW
HQ — J. Wong · 09:15
Tool life drops ~18% vs 316L — factor into cost model.
RK
Johor — R. Kumar · 10:02
Can we get variant 3 parameter sheet? Setting up CNC trial this week.

Mobile app — shop floor NEW

AI co-pilot, DFM access, and NCR logging for production engineers on the floor

New in v2.0: React Native mobile app for iOS and Android. Neither CL nor PL offer this. Designed for production engineers who need AI intelligence on the shop floor — not just at a desk.
AI Co-Pilot
IEA MobileJ. Wong ●
What SOP do I use for the current P-4421 job?
Use SOP-MACH-022 Rev 3 for P-4421 turning. Key note: bore inspection requires 2hr cooldown hold per SOP-QC-114 §3.2.
Is there a DFM concern I should know about?
Yes — Rev C bore tolerance ±0.03mm. Route to M-07 only (Cpk 1.48). Do not use M-05 for this job.
AI co-pilot on the floor
Log NCR NEW
New NCRCancel
Part number
P-4421
Issue type
Dimension out of spec
Description
Bore Ø100 measured 0.04mm over tolerance after cooldown…
Photo
📷 Tap to attach
Submit NCR
NCR logging from the floor
Notifications NEW
IEA — Notifications
DFM issue — P-6001
Undercut detected at Z-45mm. Action needed before production.
2 min ago
Drawing updated — P-4421 Rev C
Bore tolerance tightened to ±0.03mm. Use M-07 only.
1h ago
Review session — sign-off needed
DR-2024-041: P-4421 Rev C awaiting your approval.
3h ago
NCR closed — P-5501
NCR-2024-0091 resolved. CAPA-2024-008 verified closed.
Yesterday
Push alerts for DFM, revisions, approvals

Implementation roadmap v2.0

18 months · 5 phases · 9 enhancements incorporated

Total phases
5
18 months total
New modules added
5
vs SRD v1.5
Build cost (v2.0)
S$592K
+S$44K for enhancements
After 50% EDG grant
~S$296K
Net client cost
5-yr ROI (with grant)
230%+
Mid scenario
Phase timeline
M1 M2 M3 M4 M5 M6 M7 M8 M9 M10 M11 M12 M13 M14 M15 M16 M17 M18
Phase 1Active
Foundation
AI co-pilot, knowledge base, search, RBAC, dashboard, knowledge graph scaffolding
Months 1–3 · S$72K
Phase 2Up next
Revision + Review
Revision intelligence, review sessions, sign-off workflow, auto-minutes NEW
Months 4–6 · S$96K
Phase 3Planned
DFM + External
DFM engine, heatmap, Cpk routing, NCR linkage, external portal NEW
Months 7–10 · S$140K
Phase 4Planned
Advanced AI
Knowledge graph, cost engine, ERP/PLM integration, mobile app NEW
Months 11–14 · S$168K
Phase 5Planned
3D + Digital Twin
Unity 3D viewer, DFM heatmap overlay, digital twin foundation ENHANCED
Months 15–18 · S$116K
9 enhancements — summary
#EnhancementPhaseCloses gap vsType
1Auto knowledge graph (passive capture)4CLNEW
2Design review sessions with sign-off2CLNEW
3DFM colour heatmap on 3D model surface3+5PLENHANCED
4Proactive lessons learned surfacing4CLNEW
5Cost estimation engine (ERP-linked)4PLNEW
6External collaboration portal3CLNEW
7Machine-specific Cpk routing in DFM3Neither competitorNEW
8NCR auto-linkage to DFM findings3Neither competitorNEW
9Mobile app — shop floor AI + NCR4Neither competitorNEW